![](https://blogger.googleusercontent.com/img/b/R29vZ2xl/AVvXsEjpRvbx7DbA-_n-pESQNpWaVW-K2aILCQ9cBb7M0x6dbam6WX1bdcO-8LGnkQnM5qYpEthS7RNghr1cfDsMmy768V2m1zv_21-KHuDapuDXNqfN0EuwhiD6I8r-iHxfWCnMwEyKV37dTc4/s400/leak+barrel.jpg)
Its a moral tale... and the moral is: pressure test everything as you go along.
I'm guilty of rushing a few bit here in retrospect. I got a bit carried away with the excitement of nearly having the pump finished and didn't pressure it at the silver solder stage. Because once you start soft soldering you cant go back and fix your bad silver solder joints.
So for the pump barrel I pumped the system down as much as I could with the backing pump and painted some shellac on to the area that was leaking. That fixed that for now. How well it stand up to the 220 degress plus, I dont know.
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Today I hooked it all up and pumped a but of water through the cooling sleeve. There was a leak there too. Actually two leaks:
One I thought I'd fixed, close to the bubbles in the top photo.
The other at the top of the sleeve. This one only became apperant when I was pumping the water through. I had tested it initally just with gravity and it was fine. But the small pressure of the pump pushed a bit of water above the inlet level and squirted out the top.
Solution:
High temperature silicone!
Fingers crossed.
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